TPI experience
Well, I will try this again, I tried replying last night and did something that lost it all. Herre goes nothing.
My saga started with a motor that had not been rebilt right before I bought it, and the TPI setup that was custom built for it was a failed atempt at a Developement project. By that I means this manifold was built 8-10 yeares ago when a lot less was known about EFI. And they actually were not way out in left field, but misguided.
So, I will tell you a little about my 409 and the TPI as it was modified and hopefully it will help you.
My 409 is a'64 HP car block with 690 heads that have been ported/polished, stainless steel valves and hard seats, roller rockers. A Sig Erson Hydraulic roller cam with 4&7 reversed, Diamond 10:1 forged aluminum pistons, bored .030 over stack rods and crank.
The aluminum TPI Manifold was built by a guy in Mississipi for S&P and had a stock 42mm throttle body, 29# injectors and a GM ECM with a custom programed chip and harness (speed/density) from S&p.
Right off the bat when the motor was rebuilt correctly per above at the Race Shop in Seymore WI and it was run in on the Dyno it became readily apparent it would hardly run with the 29# injectors so they were swapped for 60# injectors and the motor was run in (broke in) successfully. but it was also apparent that the manifold was incorrectly built as I said before, the volume of the plenum was only 198 cubic inches and the throttle body was alying right on the #1&2 runners causing air starvation and an extremely rich condition in #1&2 and a very lean condition in #7&8. these were so far out of balance the gm ECM could not compensate and balance the fuel load. So at that point we trashed the GM "system" in favor of an accel DFI Thruster setup that would sequentially and indvidually fire the injectors and allow the pulse width to be changed individually to balance the motor. At this point with long tube headers we could make 435 HP and as i said with my block huggers and 2-1/2" exhaust it put such a resriction on the motor that the HP fell to 365HP.
So now we determined that we were not getting enough air into the motor or out of it either. So having read all I could and with advice from the Race Shop we endeavored to increase the displacement of the plenum from 198 to approximately 403 cubic inches, go to a BBK 58mm throttle body and build custom long tube headers with 3" exhaust to fit my 35 Chevy and that done made 512 hp on the dyno.
We knew that we were :missing: about 70 HP with the restrictions present and I WANTED that HP. Understand too this is a streetrod not a racecar!!
But perfomance is performance and if the motor is capable of it it should DO IT,
So, i dont know if your setup is as far out of wack as mine. but I do know this, if the motor was not on the dyno when we started it and got it balanced it was eunning good and sounding good, and for most street applications it probably would have been fine, but now I KNOW it is at its potential for how it was built.
Aceel, Fast, Howell Engineering the setup mentioned above are all great systems, each has its strength and weakness. Charlie Sykes at the Race Shop is very knowlwedgable and a great guy to talk to. They use fast software in their Alcohol race car and Accel stuff on their Dyno and fro other apps. Call them if you want they can help, and they understand the 409's as well. 920-833-1188. attached are the before and after shots of my setup.
Big Jim