Good news! Using Don's suggestion about milling and using my extra C clamps did the trick. I made 3 perfect double flares so far so I'm convinced. I milled 10 thousandths off one side, put on beefier washers and tried it but it slipped again! I noticed the tool was actually bending itself around the tube now and not closing all the way so I put 2 C clamps on and it worked. Just saved myself $400 And best of all, NO LEAKS!
BTW, there was no sign of wear on this tool. The grooves in each opening are still present and look good. It just needed the "bigger hammer" approach!
BTW, there was no sign of wear on this tool. The grooves in each opening are still present and look good. It just needed the "bigger hammer" approach!